I was the first one from our school to get to fullerton before anyone else. I tested the color sensor and saw that it was working great and demonstrated to many of the RSCC members.
When mason came with his daughter i was instructed to law the competition field out side in the hall near the elevator with the help of Edgar. when i begain to upload the code i had edited last night the robot was acting weird and would only want to go into the "if i'm on a black line " mode. it was so fraustrating and with the little time i had i could not fix the problem.
when it was our turn participate in the compotition our robot was still stuck in that loop. i figured it was the line sensor which i thought was working perfectly. during the compotitoin i uploaded the old "FAIL SAFE" code that i gave to Rangi which was code i knew worked. when i uploaded the code it was still going into the same phase. In a sence that day was a huge bust.
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